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						| Project Log:  Thursday, September 29, 2011 
 After additional research into my engine options, and 
						the input of Joe at Sound Marine Diesel, I decided to 
						install the Beta 38 instead of the 43.  I'd been 
						leaning this way for a few weeks despite my earlier 
						direction featuring the 43, but in the end there seemed 
						no particular advantage to going with the larger, 
						heavier Beta 43; the boat needed nowhere near that much 
						horsepower in a theoretical sense, but translation of 
						the available power to the water efficiently was what 
						would be important.
 
 With Joe's help and advice, we spec'd the new engine 
						with a 2.83:1 transmission turning an 18x13 3-blade 
						propeller, which combination would be effective at 
						maximizing engine power to the water.
 
 Advantages to the choice of the 38 vs. the 43 were that 
						the 38 was a bit shorter in overall length, and, more 
						importantly, nearly two inches less tall, which meant 
						that it would be a clean, easy fit in the engine room, 
						with ample clearance beneath the floorboards and 
						insulation.  I would have made the 43 work if it'd 
						been the right choice, but was happier to have 
						additional room to play with.  Additionally, the 38 
						was approximately 150 lb. lighter.
 
 I placed the order for the engine, along with an 
						upgraded alternator and belt system, remote coolant 
						header tank, remote oil filter, Adverc alternator 
						controller, and sundry additional options.  It'd 
						probably be 8 weeks before delivery.  I was excited 
						to have it on its way, however slowly.
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						| With this decision made, and the new engine on its way, 
						I constructed a new template to aid in the engine 
						installation.  I already knew the engine would fit 
						in the engine room and on the engine foundations (with 
						modification to their height, as determined earlier), so 
						at this stage of the game building the template was more 
						of an academic exercise, though I'd use it later for 
						critical measurements in modifying the foundations and 
						engine placement.
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						| These photos of my two templates--Beta 43 (right) and 
						Beta 38 (left)--show the clear length and width 
						differences between the two engines, though the height 
						and weight reduction of the 38 were the most important 
						differences for this particular installation.
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						| The 14.5" height of the 
						"engine" above the top of my template fit clearly 
						beneath the support beams for the pilothouse sole.
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						| I set the template aside for later use, and, while I was 
						in the engine room, turned to the water heater, which 
						I'd ordered recently and had on hand.  I chose an 
						Isotemp Basic 24,a 6.4 gallon unit fired by internal 
						coils plus AC electrical power (if available).
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						| Discovering how realities work in three dimensions, 
						versus dimensional information and drawings, is 
						frequently eye-opening.  I'd carefully measured the 
						space available for the water heater (an open area on 
						the port side of the engine room, aft of the saddle 
						tanks) on several occasions, and the space itself 
						offered plenty of room.  And there was no clearance 
						issue maneuvering the tank into the space.  Where 
						things went south, however, was the realization that if 
						I built a horizontal platform to support the tank, the 
						platform itself would impede maneuvering the tank into 
						or out of position. Not only did I need to get the tank 
						in in the first place, but I also wanted to ensure I 
						could remove it someday if needed.
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						| This caused me several moments of consternation as I ran 
						through my options.  One thing I'd been considering 
						since the tank arrived, however, was mounting the tank 
						vertically on the aft bulkhead of the tankage space; 
						vertical mounting was possible with this tank and its 
						rotating brackets.  Indeed, the tank fit in this 
						space fairly well, and this offered the additional 
						advantages of being easier to install and remove, and 
						also obviated the requirement for an additional 
						structural platform.
 
 The disadvantage was that this option mounted the tank a 
						little higher than I might have liked.  I was 
						trying to keep the tank as low as possible, which would 
						ensure the most options for mounting the engine's remote 
						coolant tank (which was required to be the highest point 
						in the coolant system).  This was assuming, of 
						course, that I'd use the engine to heat the water tank 
						in addition to my (still in planning stages) separate 
						diesel-fired hydronic heater.
 
 Eventually, and seeing no particular option that I 
						liked, I elected to move forward with the water heater's 
						installation on the vertical bulkhead.  To optimize 
						access to the various connection points on what would 
						become the bottom of the tank once it was in its final 
						position, I rotated the brackets something over 90° from 
						their original, factory position (as seen in the photo 
						of the heater above).
 
 The bulkhead was only 1/2" (12mm), and there was a cleat 
						on the inboard edge that was in the way of the tank, so 
						to add strength, thickness for fasteners, and provide 
						the support the water heater needed I built a laminated 
						plywood block from a layer of 18mm and 12mm plywood 
						glued and screwed together with epoxy. I marked the 
						water heater's base locations on the surface, and 
						drilled small pilot holes for later reference.
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						| I installed the new support on the existing bulkhead 
						with more epoxy and screws, then painted out this final 
						area so I could continue with the water heater 
						installation in the immediate future; I saw no reason 
						not to secure it in place now and get it out of the way 
						on the shop floor.  I planned no permanent 
						installations that would impede access to or removal of 
						the tank for servicing later.  All in all, the 
						final position seemed an acceptable compromise given the 
						intricacies of the situation.
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						| Total Time Today:  4.25 hours
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